…because I can. I thought this little project was a bit out-of-the-ordinary (if not a little nuts) and worth sharing here. No Big Point, it’s just something I’ve been working on and am getting a bit excited about. Background. About a year ago, when I started planning my first railroad, I decided I really just had to have: code 250 rail, nickel silver, and standard gauge. I was unable to find ready-made flextrack with these specs, or maybe I just didn’t like what I was able to find at the time. In any case, I’ve been struggling with the hand-laid track decision ever since, especially with spiking. For the past year, I’ve played with a number of ideas, including the stamping of one-piece rail retainers from sheet metal, milling tie plates from the solid, and solder-assembly of sheet metal pieces to form what would look like an extrusion to be cut into short pieces. After getting some casting experience, I thought I’d try going that way. The master pattern, made from a total of 14 pieces of styrene. Two pieces were laminated for the tie itself, then each cleat is made from 3 separate pieces skillfully hand-crafted to get the shape I felt would hold the rail, allow the rail to be easily inserted, and would release the mold without tearing it up.
This is just a fuzzy closeup of one end of the tie:
The master was used to make an initial mold, from which 10 castings were made. The castings were then cleaned up and used to build the master for a 10-cavity mold shown here:
The 10-cavity mold was then used to pour the ties, and in this case I used Smooth-Ons Task 7 moisture-resistant urethane plastic, dyed with both black and brown pigment:
This shot shows two of the finished ties with my rail gauge attached, just to show how the ties will work in practice–should I decide to go forward producing these for myself.
So far, I’ve pounded out about 100 or so ties, and the demold works well. Task 7 is more ‘adherent’ to my styrene backing plate than the Smooth Cast 300 resin I’ve been using until now, and that seriously slows down production. Cleaning up the backing plate prior to the next cast is taking way too much time. The Task 7 product has a good pot life–close to 7 minutes–which is good in this case because my only available method for clearing bubbles from the cleats is to probe each cavity (4 times each). Plenty of time to do that with this resin. The downside is, the demold time is about 30 minutes, vs the 8 minutes I was seeing with Smooth Cast 300. What I need to find is a long pot-life short demold plastic, but the two kind of go hand-in-hand.