A while back there was a discussion about ball bearing inserts for the truck journals. That discussion reminded me that I had purchased 50 ball bearing inserts from Great Big Trains quite a few years ago. I had never gotten around to installing them in any of my trucks. I have a few freight cars that are real stones, they just will not roll well. So I decided that I should start upgrading those cars with ball bearings. The cars I have the most problems with are the USA wood side and 1:24th steel side cars that I run. They are kind of heavy, and my LGB Moguls can only haul so many up to the summit.
50 bearings would not do all of the USA cars that I had, so I went looking for more bearings. The going price seamed to be about $1 to $2 each, At that price, I cant afford to update many cars. Then on Ebay (groan) I found a supplier that was selling them for $6.79 for a set of 10. So I ordered 100 of them.
Note The Aristocraft bearings were 3.1mm x 2.5mm x 6 mm. So you were right Greg.
Today I started upgrading some cars to see how easy it is, or isn’t. I took a USA boxcar that I knew was a stone, and I placed it on the track in Shannon. That track is a constant 2.58% grade. The car rolled about 10 inches and stopped. So I took the truck side frames off of the car and went to install the bearings. The bearings will not fit into the trucks as they are. I had to drill out the axle holes to accept the ball bearings. So I put a 15/64th drill bit into my drill press. It’s the closest size I have to 6mm without going over. I was trying to figure out how to hold the side-frames flat while drilling, and then it came to me. I could just rest the flat part of the side-frame, between the journal and the springs, on one side of the drill press vice, and with the jaws set to barely hold the journal, I should be able to hold the journal in place for drilling. I only need to drill deep enough for the 2.5mm wide bearing to press fit into the journal. Since the bearing has a flange on it, I don’t even need to drill quite 2.5mm deep.
Resting the side-frame on the vice, I was able to drill out the journals and then press the bearings into place. Then I reassembled the USA trucks, with USA wheels and put the car back onto the track in Shannon. The call rolled all the way to the bottom of the hill, probably a good 20 feet, and then rolled about halfway through the flat reverse loop before finally coasting to a stop.
On the Aristocraft trucks it’s even easier to install the bearings. I took a dental pick and just pulled the plastic insert out, and pressed the bearings into place.
But when I went to install the Aristocraft wheels I ran into a problem. The Aristo axles are larger then the USA axles, and they would not fit into the bearings (see note above). So I turned down the axles, with a file and sandpaper, until they fit. Since it was more effort then I wanted to put into this project, at this time, the test Aristo car only got ball bearings in one truck. Even with only one truck upgraded to ball bearings, the car went from rolling only about a foot on the grade, to rolling all the way to the bottom. It rolled a bit slower then the USA car, and it didn’t roll as far through the reverse loop, but the darn thing did roll on its own.